Analisis Efektivitas Mesin Disch Caller Menggunakan Total Productivate Maintenance (TPM) Studi Kasus : PT. PM
DOI:
https://doi.org/10.37090/indstrk.v9i2.1951Abstract
This research aims to analyze the effectiveness of the Disch Caller machine at PT. PM by applying the Total Productive Maintenance (TPM) method. The method includes calculating the Overall Equipment Effectiveness (OEE) to measure machine performance and analyzing the Six Big Losses to identify productivity losses. The results show that the average OEE value of the Disch Caller machine is 69.15%, which is below the international standard of 85%. The analysis of Six Big Losses identified major losses, including reduce speed losses and equipment failure losses. These losses are caused by insufficient preventive maintenance, substandard material quality, and suboptimal working environment conditions. The proposed improvements include implementing a more disciplined preventive maintenance schedule, controlling material quality, and improving the working environment. Additionally, providing operator training and enhancing coordination between the maintenance team and operators are recommended to support machine effectiveness. Implementing these strategies is expected to increase the OEE value, reduce downtime, and enhance the production process at PT. PM.
Keywords: Disch Caller, Overall Equipment Effectiveness, Productive Maintenance, Six Big Losses.
Downloads
References
Ari, D., Baineo, N., Budiharti, N., Adriantantri, E., Program, ), & Industri, S. T. (2021). ANALISIS PRODUKTIVITAS PROSES PRODUKSI MENGGUNAKAN METODE OBJECTIVE MATRIX (OMAX) DI UD. MARS MEBEL. Jurnal Mahasiswa Teknik Industri, 4(2).
Kesuma, R., & Muhimatul Khoiroh, S. (2024). Continuous Improvement dengan PDCA pada Produksi Sabun Batang di PT XYZ. Surya Teknika, 11(1), 118–127.
Ma’rup, Z. (2017). Evaluasi Penerapan 5S dan Total Productive Maintenance Untuk Meningkatkan Nilai OEE Pada PLTMG (Pembangkit Listrik Tenaga Mesin Gas).
Ririh, K. R. (2021). Analisis Risiko Kecelakaan Kerja Menggunakan Metode HIRARC dan Diagram Fishbone pada Lantai Produksi PT DRA Component Persada. Go-Integratif : Jurnal Teknik Sistem Dan Industri, 2(2), 135–152. https://doi.org/10.35261/gijtsi.v2i2.5658
Setiana, A. F., & Murnawan, H. (2024). Perencanaan Tata Letak Gudang dengan Prinsip 5S (Seiri, Seiso, Seiton, Seiketsu, dan Shitsuke) Pada PT. Aneka Coffee Industry Guna Meminimalkan Waktu Pencarian di Gudang. Jurnal Teknik Industri Terintegrasi, 7(3), 1489–1500. https://doi.org/10.31004/jutin.v7i3.28878
Sigit Nurdianto, N., & Purnama, J. (2025). Investasi Perancangan Alat Pemberi Pakan pada Ayam Secara Otomatis guna Meningkatkan Produktivitas Kerja. INDUSTRIKA, 9, 295–302. https://jurnal.utb.ac.id/index.php/indstrk
Syafri, M. H., & Murnawan, H. (2025). Pemanfaatan Optimal Limbah: Inovasi dan Teknologi Pembuatan Briket dari Ampas Kopi dan Kulit Ari Kelapa. IDUSTRIKA, 9, 303–313. https://jurnal.utb.ac.id/index.php/indstrk
Tekendo Djoukoue, G., Olabhele Esangbedo, M., & Bai, S. (2024). Ishikawa Diagram, Gray Numbers and Pareto Principle for the Analysis of the Causes of WEEE Production in Cameroon: Case of SMEs Implementing ISO 14001:2015. Journal of Management Science & Engineering Research, 7(1), 22–42. https://doi.org/10.30564/jmser.v7i1.6030
Teknologi, J., & Sastriawan, A. (2024). Penjadwalan Pemeliharaan Mesin Produksi Menggunakan Reliability Centered Maintenance. Jurnal Teknologi, 14(1), 23–35. https://doi.org/10.35134/jitekin.v12i1.113
Zaqi Al-Faritsy, A., & Suluh Wahyunoto, A. (2022). Analisis Pengendalian Kualitas Produk Meja Menggunakan Metode Six Sigma Pada PT XYZ. Jurnal Rekayasa Industri (JRI), 4(2).
Zuhrotusy-Syarifah Qurrotu’aini, & M. Ardan. (2023). Analisis Fishbone sebagai Implementasi Solusi Penggunaan Tempat Tidur Belum Ideal Rumah Sakit. Jurnal Pengabdian Kepada Masyarakat Nusantara (JPkMN), 04(2), 775–782.
Ma’rup, Z. (2017). Evaluasi Penerapan 5S dan Total Productive Maintenance Untuk Meningkatkan Nilai OEE Pada PLTMG (Pembangkit Listrik Tenaga Mesin Gas).
Eky Aristriyana, & Rizki Ahmad Fauzi. (2022). ANALISIS PENYEBAB KECACATAN PRODUK DENGAN METODE FISHBONE DIAGRAM DAN FAILURE MODE EFFECT ANALYSIS (FMEA) PADA PERUSAHAAN ELANG MAS SINDANG KASIH CIAMIS. JURNAL INDUSTRIAL GALUH, 4(2), 2022.
Isniah, S., Hardi Purba, H., & Debora, F. (2020). Plan do check action (PDCA) method: literature review and research issues. Jurnal Sistem Dan Manajemen Industri, 4(1), 72–81. https://doi.org/10.30656/jsmi.v4i1.2186
Downloads
Published
Issue
Section
License

This work is licensed under a Creative Commons Attribution-ShareAlike 4.0 International License.